Moreover, increasing the RMP with setSpeed has no visible effect. I changed the number of steps in each direction, tried with the function oneStep(direction, step-style) in a loop and tried with an other motor but the result is always the same. I also tried sapping the cable pairs around to no avail. The movement when using Microsteps is seem smoother but I can still feel the motor blocking from time to time. ![]() ![]() When the program uses Single steps the motor going back is almost visible. The motor turns in one directection and then the other as expected but the rotation is very slow and jerky as if the motor was going forward 2 steps and 1 back constantly. ![]() l#overview) everything to work with the same model of nema17 stepper motor you have on the website.Īfter installing the software and finding the right pairs of wires, I tried the stepperTest.py file. I recently bought a DC Motor & Stepper Motor HAT from you and installed (following.
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